北京航空航天大学学报 ›› 2013, Vol. 39 ›› Issue (8): 1091-1095.

• 论文 • 上一篇    下一篇

新型主动液压滤波器的设计与分析

荆慧强1, 张晓宁2, 李艳芬3, 付永领4   

  1. 1. 北京航空航天大学 自动化科学与电气工程学院, 北京 100191;
    2. 北京大学 信息科学与技术学院, 北京 100871;
    3. 北京强度环境研究所, 北京 100076;
    4. 北京航空航天大学 机械工程及自动化学院, 北京 100191
  • 收稿日期:2012-09-07 修回日期:2013-04-12 出版日期:2013-08-30 发布日期:2013-09-03
  • 基金资助:

    科技部国际合作资助项目(2010DFA7254)

Design and analysis of a new kind of hydraulic active filter

Jing Huiqiang1, Zhang Xiaoning2, Li Yanfeng3, Fu Yongling4   

  1. 1. School of Automation Science and Electrical Engineering, Beijing University of Aeronautics and Astronautics, Beijing 100191, China;
    2. School of Electronics Engineering and Computer Science, Peking University, Beijing 100871, China;
    3. Beijing Institute of Structure and Environment Engineering, Beijing 100076, China;
    4. School of Mechanical Engineering and Automation, Beijing University of Aeronautics and Astronautics, Beijing 100191, China
  • Received:2012-09-07 Revised:2013-04-12 Online:2013-08-30 Published:2013-09-03

摘要: 针对目前主动液压滤波器体积大、结构复杂等问题,提出了一种占用空间小、结构简单的新型主动液压滤波器. 采用计算流体动力学在时域内对滤波器所载流体域进行了压力分布计算,分别对三组可控参数激励位移幅值Dm及频率fm作用下的流体域进行分析,通过比较分析发现,Dmfm的选择决定着该液压滤波器性能的优劣,如果二者与原始非定常流幅频特性匹配较好,则该液压滤波器滤波效果良好,反之,会使系统压力脉动变的极不稳定,这与波的干涉原理相互吻合. 算例计算结果表明,当激励频率与初始非定常流频率重合达525 Hz,且激励幅值达0.05 mm时,系统的压力脉动峰峰值可从2.26 MPa降到0.25 MPa,即脉动从±5.38%降至±0.6%,说明了该主动液压滤波器的有效性.

Abstract: In view of the current hydraulic active filter of large volume, complex structure and other problems, a new type of hydraulic active pressure fluctuation filter (HAPFF) was present with simple structure and small volume. The method of computational fluid dynamics (CFD) was employed to investigate the pressure field distribution in time domain and three group data of Dm(excitation amplitude) and fm(excitation frequency) were involved. The results indicate that the performance of the HAPFF depends on Dm and fm, if they match the equivalent parameters of the original unstable flow rate, then the HAPFF perform well, which agree with the wave interference well. The calculation denotes that the peak-peak pressure value reduced to 0.25 MPa from 2.26 MPa when fm=525 Hz and Dm=0.05 mm (that is to say, the pressure fluctuation dropped to ±0.6% from ±5.38%), which verify the effectiveness of the proposed design.

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